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AC 175D Front Axle Kingbolt

Printed From: Unofficial Allis
Category: Allis Chalmers
Forum Name: Farm Equipment
Forum Description: everything about Allis-Chalmers farm equipment
URL: https://www.allischalmers.com/forum/forum_posts.asp?TID=184551
Printed Date: 19 Jul 2025 at 3:56pm
Software Version: Web Wiz Forums 11.10 - http://www.webwizforums.com


Topic: AC 175D Front Axle Kingbolt
Posted By: BigGuy1000
Subject: AC 175D Front Axle Kingbolt
Date Posted: 12 Nov 2021 at 10:34am
We have an AC175D with oscillating wide front axle pivoting on a steel rod hung on 2 trunnions under the frame of the tractor.  On one trunnion is a 3/8 Grade 8 kingbolt to keep the rod in place in the trunnion.  This bolt breaks at the end of the threads quite often, may last 1 month or 3 months or a year, but always breaks at the end of the threads of the bolt.  There are no grease fittings in the trunnions!  We do oil often but apparently not enough, as it does not prevent breakage.  I did try to drill 1/8 in hole in trunnion to install a fitting but there is a very hard bushing thru which I cannot drill with ordinary drills and hand tools.  Does anybody have a proven solution to this problem which will keep the rod in place?  This sort of wide front axle is common on many AC tractors.
TNX in advance!!!!




Replies:
Posted By: DrAllis
Date Posted: 12 Nov 2021 at 12:08pm
New Gr8 bolt and locknut. Weld the big pin to the axle on the front. Fixed.


Posted By: BrianC
Date Posted: 12 Nov 2021 at 12:23pm
Talking about axle failures here:
https://www.allischalmers.com/forum/bad-day-for-175_topic56642.html" rel="nofollow - https://www.allischalmers.com/forum/bad-day-for-175_topic56642.html

The online parts book appears to show that this bolt was upgraded to 1/2"
diameter at some point. I don't have a clear view of the assembly. I imagine
the bolt retains the pin in the front support, I just can't figure why it should break.
You are talking about lubrication, is the pin all galled up and seized to bushings?

My 160 has grease fittings.

Someone who knows will speak up.





Posted By: MACK
Date Posted: 12 Nov 2021 at 9:03pm
Use bolt like the Dr. Said with lock not but don't tighten it tight.                 MACK


Posted By: DrAllis
Date Posted: 12 Nov 2021 at 9:31pm
They eventually went to the larger 1/2" bolt because of the failures with the 3/8" bolt being sheared off. This is due to too much rotational drag on the large pivot pin, especially with a loader. What you don't want is the pin to fall out. You can probably drill it out to 1/2" if there's enough meat there to work with. But if you weld the pin on the front with a new bolt in the rear it will never fail. Why will you ever need to remove that pin ?? You won't.


Posted By: BrianC
Date Posted: 14 Nov 2021 at 11:43am
Was the 1/2" bolt upgrade a sure fire fix? Lady farmer (35miles away) has a 175 and I would take a look for her. No loader, just some weights for plowing.


Posted By: DrAllis
Date Posted: 14 Nov 2021 at 11:54am
I'm sure they thought it was, but unfortunately who within the A-C company ever followed up on such a problem after they quit making the tractor ??  NO ONE did!!  I'm sure it was an improvement regardless. They had the same issue on the 7000 series and finally went to a snap ring on the rear of the shaft instead of a thru bolt. On the front of the pivot shaft they welded a 1/4" x 3" x 3" square plate to it. Then, they welded a piece of keystock to the axle frame up against the square plate. This kept the pivot shaft tied to the axle framework as far as turning, but by removing the snap ring at the rear, one could remove the pivot shaft. That was a good fix. I have done that on some maroon chassis tractors while still leaving the bolt in the rear and I have welded many other solid to the axle frame at the front, while leaving the bolt at the rear. Again I ask...….why would anyone ever want to remove that pivot shaft ???????????


Posted By: BigGuy1000
Date Posted: 10 Jul 2022 at 8:43pm
Applied the above bolt (3/8 X 3 1/2 GR8 NF, GR8 fine nuts with 1/2 in long bushing) to the ac175D trunnion.  Bushing is next to the trunnion.  Nuts are tight against each other, but are backed off one full turn from the bushing.  The threads are entirely outside of the trunnion.  It has not broken in more than 2 years now on loader duty!
I will declare this fixed, WITHOUT needing to buy or learn a big expensive welder!!!!



Posted By: DrAllis
Date Posted: 10 Jul 2022 at 10:11pm
November 12th 2021 till July 2022 is only 8 months by my math.


Posted By: SteveM C/IL
Date Posted: 11 Jul 2022 at 12:50pm
....time flies??????



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